Update on the beam change. I won’t detail everything as it’s been covered before, just the new things I found out as I went along. To bullet point the sequence I took though:
• Remove everything.
• Fit the new beam, with latch at B post and tighten front hinge bolts
• Remove Latch and fit door shell ( with Window and frame in my case – see below)
• Align door to body / Check frame is sealing on rubbers
• Rebuild the rest.
A repairable beam came from Lotus Bits. Aware of the potential differences on opening angle, I made sure I got a beam including hinges and strap. I now know a lot more about the differences ( See thread link in earlier post). If I did another one, I would modified the check strap location points to get the wider opening, - Too late now.
The ‘new’ beam was not without corrosion (find one without if you can – I know new ones can are available, but where’s the fun in that !). It was solid enough to cut out the rust and set in new metal. I prepared the replacement metal inserts, but entrusted to a professional to do the TIG welding. The beam still went a bit banana shape. I suspect it would be impossible for the heat not to introduce some bend, but it’s all gone together without much grief so slightly wonky isn’t the end of the world. Before rebuilding though, I did make sure the attachment points for the window frame were all on the same plane
Was fortunate that most bolts came undone as they are meant to ( with a spanner). Only two exceptions : -
• The two front bolts that hold the door skin to the beam (via the angle plate) – they just turned. Angle grinder with slitting disc took the heads off these bolts. Removing the check strap front bolt allows easier access.
• The top front window frame bolt that turned with a stripped thread. Reason : the bolt used was too long. It had bottomed out on the boss that holds the check strap on a wide opening door. Fortunately because it had bottomed before clamping the frame, there was room to get a hacksaw blade in – just.
Once all was loose, and most importantly removing every last possible item to get as much room as possible inside the door, try as I might, I just couldn’t get the drop window out of the frame, nor the frame with window out of the door. Tried all sorts bar really over stressing the frame legs to take the window out, then ended up with the frame (with glass still in ) really high at the rear, as in photo below:
Time for a coffee, and on return I begin to wonder if I can slide the Door shell (with window frame and window still in) off the beam whilst it sits this high. Pleased to report you can

. The parts are a bit unwieldy once removed. Care needed not to over stress the fibreglass (supported the frame once laid down), but it worked. The window frame legs need to be high enough to clear the notch in the door beam end plate (where the internal door release lever sits over) but it can be done.
Beam change and rebuild was straight forward, but would have been MUCH harder without the “nut plate” I’d made for the front shell mounting (worth it’s weight in gold). You can see it in the photo below (black bar hanging under the angle plate).
Without this plate, I really don’t know how I would have got the top bolt in. With the plate, it was easy to offer up the plate to get the lower bolt started, then just swing until the top bolt was found and started. I put a second nut on the lower bolt after tightening to lock the thread, but no way could I have reached the top position to do the same. I’m sure it will all stay tight – Won’t it?
Body alignment and door striker setting all went without hitch, but I struggled with getting the window to slide smoothly. About half way down, it went very tight. A strip down and regrease of the operating arm improved things, but in the end, I went for completing the job, accepting that I’d revisit this problem later. It’s the window in the channel that is the problem and it was never good. I have a spare frame, and also the original glass for the car ( the U channel for the drive roller rotted out years ago apparently), so a job on the back burner for now.
Last item was to repair and fit properly the 3 removable panels from the inside door shell. Sorry, but I’m a bit pedantic about bodged work, using a mix of wood screws, tape, sealant, self tappers and glue. Further, the largest panel at the front covering the window motor was never fitted properly by the factory. It is profiled to fit into the shape of the door shell, but hadn’t been cut back far enough at the rear to clear the internal door lever, so sat too far forward. As a result it needed about 8mm of sealer between it and the door shell in places. Much better now, with M4 screws into a tapped Ali plate behind in most positions, and clips / stainless steel self tappers where this proved impossible. – The fully assembled door feels very solid and no rattles ( unlike the drivers door !). As my thread title, one job jobbed, another one found – rebuild the drivers door properly!
Final learning, next time I’d set the beam about 1mm high with reference to the striker when just the beam. Once all the weight is back in the door, it drops about 1-2mm.
Tony